|
|
|
This is the pump we decided to try. It's variable speed and can have a range of 28 to 800 ml/m with the 0.25 inch tube. 65 ml/m is about 1 gph.
|
Ran some initial pumping tests. It can pump some very viscous and dirty material. This looks very promising.
|
The flow appears to be about a gallon or a little more per hour. It's been running for about 45 minutes. The stream appears very smooth.
|
|
|
|
This photo should give you an idea of the particulate that this oil contains.
|
After two hours the pump moved about 2.5 gallons of some very nasty oil through the centrifuge.
|
I normally wash my buckets with a little diesel fuel. Here you can see how it thinned out the junk in the bottom of the bucket.
|
|
|
|
This is the bucket after draining off the mix. Notice how a lot of the particulate dropped out readily.
|
This doesn't look good. I suspect the tubes are blocked. This is why the new design moved away from the tubes.
|
This is the top half of the rotor. Note the water dripping off.
|
|
|
|
This is the bottom half of the rotor. This is after only 2.5 gallons of super nasty oil.
|
This is some thick cake.
|
Note how the cake is thicker at the tubes.
|
|
|
|
See how dry the cake is.
|
The tubes were definitely plugged. The feed cone shouldn't have been full of oil.
|
I scraped all the cake out of the rotor and weighed it, 254 grams or about 9 ounces, better than a half pound.
|
|
|
|
This is the cake. I tried to not get too much liquid oil.
|
This is the contents drained from the rotor on shutdown. Note how much water was captured by the centrifuge. I'm estimating about 500 ml between the two bottles.
|
This is after the second pass. Notice that the feed cone is clean, no back feeding this time.
|
|
|
|
The material on the outer wall is very soft, almost like grease or thick gear oil.
|
Removing some of the soft material reveals a very thin particulate layer. This is likely due to the plug feed tubes on the last run.
|
This is the top from the second run.
|
|
|
|
Scraped out the waste from the rotor wall. Very soupy this time.
|
This is the waste collected on the second run. This is 158 grams. Because this time the sample is so wet, it may not be a good comparison with the first pass.
|
On the third pass I didn't take the machine apart to weigh the waste. It did form a thin layer of heavier grease but I don't see any particulate layer. This is likely what the second layer would have looked like had the feed tubes not plugged.
|
|
|
|
After running all the tests with the oil I decided to mix the wash diesel with the drained oil and see how it pumped. You can see it was fairly chunky. Pumped fine. No problems.
|
This is the bottom half of the rotor. The diesel slop mix didn't dissolve the grease layer but it certainly piled up the gunk.
|
This is the final result after running the diesel wash mix. The grease layer remained and the particulate was built up behind.
|
|
|
|
Came in the morning to find the pump was leaking oil all over the floor.
|
This is how the hose split. This happened after about 4 days of running.
|
Tygon® F-4040-A Lubricant & Fuel Tubing
Specifically designed to handle most fuels and industrial lubricants, Tygon F-4040-A lubricant and fuel tubing resists the swelling and hardening caused by hydrocarbon-based fluids. This significantly reduces the risk of failure due to cracking and leakage. Its minimum extractability safeguards the liquid or vapor being transferred against adulteration.
Tygon F-4040-A is translucent yellow for positive identification and to allow easy flow monitoring and is routinely used to handle gasoline, kerosene, heating oils, cutting compounds and glycol-based coolants.
|
|
|
|
About 10 years ago I started experimenting with the use of a peristaltic pump. It worked really well but after a tube failure, and the subsequent spill, I gave up. Recently, I started using Tygon® F-4040-A tubing. So far it is working great. Note the containment, just in case.
|
Today when swapping drums I couldn't get the pump to prime. It turns out my pump is designed for 3/32nd wall thickness tubing and the Tygon tubing is 1/16th. I was able to get it working by shimming the tube with some card stock.
|
|