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Here is the tank ready to be modified.
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Started by using the band saw to cut off the bottom end bell so I can flip it around.
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After cutting, I tacked some angle iron to the end bell and drove it out of the cylinder.
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This is the end bell removed.
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Next the end bell was bored and faced in preparation for the bung to be welded on.
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Bung was welded onto the end bell on the rotary table.
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After some time I was able to install the end bell into the cylinder in the desired orientation and welded it on using the rotary table.
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After welding was completed the tank was evacuated of all the air and hydrostatically tested using the garden hose. This isn't a pressure vessel but 50 psi water finds leaks in a hurry. All the welds were sound but there was a crack from one of the tack welded pieces I used to drive the bell square.
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Quickly welded the leak and re-tested. Held and leak free.
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I then welded on some angle iron legs and an eighteen inch disk for the base. This will allow me to move it around by rolling like a bottle. Note the plugs in the valves, just in case. Nobody likes leaks. Remove when needed. Too easy to bump a valve in a busy shop.
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This is a view looking down. With the legs it's 6 feet tall and requires a step ladder to fill.
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Cut a 2 inch hole in the top with a hole saw. The inverted end bell serves double duty as a funnel.
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After filling the tank with all the mixed oil I had on hand I let it sit for a few days before cracking the valve and draining the water.
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I ended up draining about 7.5 gallons of water from the 20 or so gallons of mix I started with. The water is very rusty and this is due to the tank. If you would have seen how dirty I was the day I built the tank... you'd understand. ;)
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